FLEX-STAR

Camilo Ontaneda

Suteera Pirom

Samer Saba

David Zetune

Instructor: C. Pastore

INTRODUCTION:

Upon the request of R Secret Designs to find the "ultimate magic fabric" for their FlexStar, a multiple armed flexible throwing toy. The purpose of our project was to find an abrasion resistant fabric, which would be flexible at the same time. Due to the nature of the toy it needs to withstand multiple skidding on surfaces such as asphalt and concrete. We continued to do this by exploring different assembly methods as well as different fabric constructions.

PROCEDURE:

The first step we took in the process was to take apart one of the toys to be able to get the existing pattern to work with. While we were waiting for samples of the real oxford nylon cloth used, we assembled a prototype out of coated polyester. The prototype was flexible, but it was so soft that it did not fly very well. Also the fabric did not have enough stiffness to help support the flex star during flight. By this, we mean that the arms of the toy twisted during flight. This fabric was obiously not the first choice but it would be good to test different assembly methods.
This process helped us in learning what the problems were during the construction. Our first conclusion was that the pods at the end of the arms were puckering due to the shape. (curved) We vowed to get rid of them to improve the abrasion of these pods. The points created by the puckering of the pods are the first part to wear out during skidding, if we eliminate them then we will make the toy much more resistant.
We believed that by moving the stitches away from the edge of the pod, the puckering would be reduced. We planned to move the stitches to the sides of the pod. With a little help of the Apparel School we asystem for making one have a larger diameter than the other. Having the smaller piece sowed on the other side would cause the stitches to be pulled away from the edge. We used tabs in order to help us sew the two un even pieces together. These tabs would be folded to make up for the differnece in circumference when sown together. The result were the following: First the two pieces were almost impossible to sew together, the process wasalso too laborious. Second the construction method did not achieve what we had hoped for. In reality it was the exact opposite.
After deciding that the construction method used by R. Secret Designs was the best, we decided to fill the pods with polyester beads. We got on the phone that very day, and ordered some from a contact the school had. The idea for using them came about because the beads are weather resistant,washable, and they will not swell up if the toy lands in a puddle. They are also round which will give the pods a better packing order. They are made out of recyclable polyester, which is very friendly for the environment. Lastly they are not expensive and that was also a big issue. Unfortunately to this day we have not received them, so we have not been able to run experiments comparing rice to polyester.
Our next idea was to make the pod out of a knit structure. In this way we would be able to remove the stitches from the sides, and therefore remover the puckering all together. This would reduce the different costs of the stitching process such as labour, sewing thread, etc. Then went to the knit lab, we needed to use a small needle gauge, 10 cut, so that the stitches would not catch and snag on the asphalt. Before building a fully fashioned version of the pod, we made a few yards of fabric so that we could do some abrasion tests. The tests were a success in most cases, the knit fabric was made from a 72 tex, 3-ply nylon yarn (Nylon 6.6 was used). The abrasion more than tripled in comparison to the oxford cloth used previously, for most cases. The exception was the inflated diaphragm test.
Then we proceeded to make a fully fashioned sample; however, we soon realized that without the appropriate equipment we would never be able to construct sample this way. The equipment we were missing was a knitting machine with presser feet, which would keep uniform tension throught the sample during knitting. We did on the other hand, make more of the fabric such as the one we tested, in order to build our models. We sewed them together following the original procedure used for the woven flexstar.
When they were constructed, we found that the 420 nylon parapack fabric worked the best. The stiff woven boddy and the new knit outside pods were the perfect combination. We think that it is even easier to throw than the original. We took the flex star apart and weighed all the peices individually. After that we made the proper adjustments to make sure that the weights of the original and the improved flex stars were the same.
The improvments we observed with the knitted outer pods were the following. Fisrt, we noticed the toy openned up faster after being released (see following figures). Second, it was easier to throw because of the way the knit fabric reacts to the centripetal forces when being thrown. The loops in the knit structure stretch allowing the toy to have more of an even circumference when in flight.

Figure 1. Picture of woven Flexstar in flight. Note that righthand spar is twisted, affecting aerodynamic response.

Figure 2. Picture of knitted Flexstar in flight. Note that spars are flat. This was observed repeatedly during flight testing.

TESTS:

The following tests were performed on the knit fabric, a single jersey, and the woven Oxford, 210,420, 730 denier nylon:

  1. ASTM D 3884 ROTARY PLATFORM, DOUBLE HEAD METHOD: The test specimen, mounted on a platform, turns on a vertical axis, against the sliding rotation of two abrading wheels. One abrading wheel rubs the specimen outward toward the periphery and the other, inward towards the center. To test the abrasion of the fabrics by using #H22 wheels. They are the roughest wheels which are available to us, they were selected to simulate concrete and asphalt.
  2. ASTM D 3886 INFLATED DIAPHRAGM ABRASION TESTER: A specimen is abraded by rubbing either unidirectionally or multidirectionally against an abradent having specified surface characteristics. The specimen is held in a fixed position and supported by an inflated rubber diaphragm which is held under a constant pressure. Our tests were conducted at 3 psi., with 3lbs. on the head. The sand paper used was 300x.
  3. ASTM D 4157 OSCILLATORY CYLINDER ABRASIVE MACHINE: Abrasion resistance is measured by subjecting the speciment to unidirectional rubbing action under known conditions of pressure, tension, and abrasive action. The sand paper used was number zero emery paper. The tension was 2 lbs. dead weight load tension.
  4. THE DRILL TEST: We developed this test specifically in order to measure the abrasion resistance of the pods which were filled with rice. The procedure followed in this test was to attach the pod to a drill and run it on asphalt and concrete. The results of testing different fabrics were reported in terms of how much time it took to break the pod.

 
 
 
 
 
 
Test Results 
Fabric  ABRESER  WYZENBEECK  INFLATED DIAPHRAGM  DRILL TEST 
No. of Cycles  No. of Oscillations  No. of Cycles  No. of Seconds 
210 Nylon Oxford  400  425  4000 *  45 
420 Nylon Parapack  1700  <<>>  <<>>  <<>> 
Nylon 82 tex (S. Jersey)  3500  750  2870  300 * 
* Fabric did not break.
<<>> Fabric was not tested

TEST SPECIFICATIONS

ABRESER: Model 503 Standard Abrasion Tester. Abrasion Test Wheels # H-22 (Calibrade).

INFLATED DIAPHRAGM: Universal Wear Tester. Pressure of 3 psi Weight of 3 lb. on head.

CONCLUSION:

The results on our knit fabric were better than we expected. We new that we would have some problems with snagging, so we used a 10 gauge knitting machine. This means that there are ten needles to an inch. This made the loops small enough that snagging was not a factor. The knit fabric had a much softer hand as compared to the woven fabric, even though we were not able to make them without the seems. We expect it to be better with this improvement. Significant improvement was in the flying time of the Flex-Star, because of the knitted structures, the beads were allowed to expand inside each pod, and as a result of that, the force distribution was even on each arm of the Flex-Star. Because of this uniformity, the air resistance was equal on each arm, and that improve the over-all flying properties of the Flex-Star. These results were reached by throwing the Flex-Star over 50 times in the air. The only negative test was inflated cylinder. The reasons for the failure of the fabric under these conditions were the single jersey structure. The pressure and abrasion on the fabric was applied only on a small area of fabric. Under these conditions one loop broke, and cause failure in the fabric due to the laddering effect. These are typical results for a single jersey fabric, but under normal conditions the toy will not be exposed to as high tensions as in this test.

SUGGESTIONS:

  1. Using fully fashioned gloves knitting machine, that will knit the whole pod and part of the arm as a whole piece without using any stitching. The only stitches needed would be the ones for sewing it to the center piece. This machine will increase production dramatically. Eliminating all the labor involved in tracing the pattern and sewing the pieces together.
  2. Using recyclable polyester beads, they are cheap, improve the packing factor, and they are environmental friendly. The will also make the toy washable. The improved packing factor will increase the abrasion resistance on the surface of the pod. This will be because less of the beads surface will be in contact with the fabric, as compared to the rice currently being used.
  3. Using glow in the dark fabric for the pods, will make it more fun to play with in the dark. It will also make it easier to catch, and see, if it is later in the day.

COST:

Yarn = $9.5/lb. for 100 lb. of yarn.
That is $20.90/kg.
The price for a 7 gram pod would then be $0.146
If the Shima glove machine is used. (cost between $8,000 new and $6,000 for used)
We estimate that the machine would knit five pods in about 4 minutes.
Annual production of the machine at 85% efficiency, 50 weeks a year, on 2 shifts, five days a week, would be 25,500 of each the five and the three point toys.
If they are sold for $11.99 and $9.99 respectively.
Therefore total retail annually would be $561,000 a year, and the utility would be $465,931 annually.
Note: These prices are using estimates of both labor and manufacturing costs. Real prices were used when ever possible.